Perbaikan Proses Bisnis dalam Alur Pembuatan Kode Identifikasi Material Menggunakan Metode Lean Service pada Perusahaan Minyak dan Gas Bumi (Studi Kasus PT XYZ)
Nia Dwi Astuti, Ir. Andi Sudiarso, S.T., M.T., M.Sc., Ph.D., IPM
2025 | Tesis | S2 Teknik Industri
Industri minyak dan gas
menghadapi tantangan dalam kelancaran operasional, termasuk pengelolaan
material. PT XYZ, sebagai perusahaan hulu migas, mengalami keterlambatan dalam
proses pembuatan Kode Identifikasi Material, dengan rata-rata waktu (lead time) 23 hari jauh melampaui service level agreement (SLA) perusahaan selama 5 hari. Hal ini
berdampak pada pengadaan barang dan kelancaran operasi produksi serta
pengeboran. Penelitian ini bertujuan untuk mengidentifikasi waste dan penyebab utama keterlambatan pembuatan
Kode Identifikasi Material, merumuskan langkah perbaikan proses, serta mengukur
efisiensi waktu yang dihasilkan dari usulan perbaikan. Penelitian ini
menggunakan pendekatan Lean Service dengan mengaplikasikan metode Seven Waste dan Service Value Stream Mapping (SVSM). Pada tahap current state, identifikasi waste dilakukan melalui Process Activity Mapping. Analisis akar masalah menggunakan Diagram Pareto
dan fishbone sebagai bagian dari metode Root Cause Analysis (RCA). Prioritisasi perbaikan menggunakan Analytical Hierarchy Process (AHP) dan Simple Additive Weighting (SAW) oleh expert. Solusi perbaikan kemudian diuji coba kepada
responden untuk mendapatkan nilai rata-rata future lead time. Hasil analisis menunjukkan bahwa waste
utama dari proses ini yaitu delay dan unnecessary movement. Waste delay terjadi karena proses persetujuan manual
yang panjang dan kurangnya sistem digitalisasi yang memperlambat verifikasi.
Sedangkan, untuk waste unnecessary movement terjadi karena banyaknya tahapan verifikasi
akibat keterbatasan akses database sehingga kataloger regional hanya berperan
sebagai perantara. Lean Service melalui identifikasi waste, analisis akar masalah, serta perankingan solusi
alternatif oleh expert terbukti mampu menurunkan total lead time
dari rata-rata 20,44 hari menjadi 6,25 hari atau efisiensi sebesar 69%
dibandingkan kondisi existing. Penelitian ini menyimpulkan bahwa
penerapan Lean Service secara sistematis efektif untuk mempercepat
proses pembuatan Kode Identifikasi Material, meningkatkan efisiensi proses dan
kualitas layanan pengadaan, serta berpotensi diterapkan lebih luas di sektor
migas.
The oil and gas industry faces significant challenges in
maintaining smooth operations, particularly in material management. PT XYZ, an
upstream oil and gas company, experiences delay in the Material Identification
Code creation process, averaging 23 days—far exceeding the company’s Service
Level Agreement (SLA) of 5 days. These delays disrupt procurement and critical
operational activities, including production and drilling. This study aims to
identify waste and the main causes of delays in the creation of material
identification codes, formulate process improvement steps, and measure the time
efficiency resulting from the proposed improvements. This study applies the
Lean Service approach by implementing the Seven Waste concept and Service Value
Stream Mapping (SVSM). In the current state analysis, waste identification was
conducted using Process Activity Mapping. Root cause analysis was performed
through the Pareto Diagram and Fishbone Diagram as part of the Root Cause
Analysis (RCA) method. Improvement prioritization was carried out using
Analytical Hierarchy Process (AHP) and Simple Additive Weighting (SAW) involving
expert judgment. The proposed improvement solution was tested with respondents
to obtain the average future lead time. The analysis shows that the main wastes
in this process are delay and unnecessary movement. The delay waste occurs due
to lengthy manual approvals and the lack of digitalization that slows down
verification. Meanwhile, unnecessary movement arises from multiple verification
stages caused by limited access to the KIMAP database, resulting in regional
cataloguers functioning merely as intermediaries. By applying Lean Service
through waste identification, root cause analysis, and expert-based
prioritization of alternative solutions, the total lead time was successfully
reduced from an average of 20.44 days to 6.25 days, achieving a 69% improvement
compared to the existing condition. This study concludes that the systematic
implementation of Lean Service is effective in accelerating the material
identification code creation process, enhancing process efficiency and
procurement service quality, and holds significant potential for broader
application within the oil and gas sector.
Kata Kunci : Kode Identifikasi Material, lean service, service value stream mapping, root cause analysis, lead time, minyak dan gas bumi.